Underhood Wiring problems of the 2001 Ford F-250

Six problems related to underhood wiring have been reported for the 2001 Ford F-250. The most recently reported issues are listed below.

1 Underhood Wiring problem

Failure Date: 04/04/2007

2001 Ford f250 crew cab spontaniously caught on fire while parked in the driveway. It was a total loss ,and serverly damaged the house and driveway. Fire crews stated the house was 2 minutes from igniting when they foamed it.

2 Underhood Wiring problem

Failure Date: 02/10/2007

The cam positioning sensor in the Ford power stroke 7. 3l diesel has gone out at 60,000 miles. This caused the vehicle to completely shut down. This was not the only truck this has happened to. Many people I know had this happen within the first 100,000 miles. Ford repaired the cps for $400. 00 at my expense. Also the o ring in the high pressure oil pump went out at 71,000 miles with no warning, causing me to dump all of the oil out. I discovered it before it caused motor problems. Ford fixed this problem for $500. 00. Both problems a were very common with the 7. 3l and need to be addressed by Ford. They were not ordinary problems and need some kind of attention from Ford.

3 Underhood Wiring problem

Failure Date: 09/06/2006

Furthest back spark plug blew while driving my 2001 Ford f250 pick-up. I only have 76100, miles on my truck the warranty just ran out the cost of repairing this is $4300. I was told that this is a factory defect and I want this problem put on the record, so that it can be investigated. I stopped driving as soon as I heard a noise and have kept my vehicle in top shape.

4 Underhood Wiring problem

Failure Date: 08/17/2006

: the contact stated while the vehicle was idle, a fire erupted which was caused by a faulty electrical system. The fire originated from the engine compartment front underhood. There were no warning signals prior to the incident. Upon inspection, the cruise control deactivation switch and wiring for the electrical system was observed to be completely burnt to the ground. A fire report was taken# 06-017205. Also, the manufacturer was notified, but would not offer any resolution while this case was under investigation.

5 Underhood Wiring problem

Failure Date: 07/04/2005

We were notified by police and fire department officials that there was a fire in our yard. Our Ford 250 was on fire and had not been driven for around 4 hours. Upon investigation the fire marshall indicated the location of where the fire began and presumed it was the brake pressure switch based on its location. The car has been totaled and caught another vehicle on fire next to it.

6 Underhood Wiring problem

Failure Date: 12/29/2004

Fire in Ford F-250 pick-up truck. Parked in garage for about 2 hours. Owner saw initial fire in engine compartment on driver's side. Remains of cruise control deactivation switch were found and x-rayed; internal contacts were splattered from electrical arcing. Fuse #13 was a 20 amp device and was the only one blown. According to Ford wiring diagrams, that circuit fed the cds. The owner reported that the cruise control quit working last summer. The dealership told him it needed a new cc module and would cost $150. 00. Owner elected not to spend the money at that time.




Safety Ratings of F-250 Cars
F-250 Service Bulletins
F-250 Safety Recalls
F-250 Defect Investigations