Ford F-150 owners have reported 84 problems related to loud engine noise (under the engine and engine cooling category). The most recently reported issues are listed below. Also please check out the statistics and reliability analysis of Ford F-150 based on all problems reported for the F-150.
Tl-the contact owns a 2008 Ford F-150. The contact stated that while driving at 5 mph,he heard an abnormal noise that came from the engine. The vehicle was taken to a dealer mechanic, who diagnosed that the timing chain, timing chain slide, timing chain tightener and cam phasers need to be replaced. The vehicle was repaired. The manufacture was notified of the failure. The VIN was not available. The approximate failure mileage was 120,000. Lb.
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Tl-the contact owns a 2003 Ford f150. The contact stated that while driving at approximately 65 mph, the vehicle made an abnormal noise and the gas pedal was depressed but the vehicle would not accelerate as the check engine warning indicator illuminated. The failure recurred two times. The vehicle was towed to the contact's home where an independent mechanic diagnosed that the spark plug detached and needed to be replaced. The vehicle was repaired but the failure recurred. The manufacturer was not made aware of the failure. The failure mileage was approximately 148,000. Sg.
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I purchased a 2011 Ford F-150 4x4 with around 41,000 miles on it from texas direct auto, on 08/18/14 with an existing warranty on it. On the morning of 09/24/14 while driving to work, I heard a loud noise and smoke starting coming out of my ac vents, hood and exhaust pipe, as well as losing power to the truck and shaking really bad. I was able to get off the freeway to park it. The truck is still under power train warranty, so I towed it to joe myers Ford, houston ,TX down the street. Long story short, I was told the motor blew and on 10/2/14 joe myers Ford is denying the warranty because I do not have service maintenance records, then I was told it was due to abuse. Joe myers Ford quotes me $10,500 to install a new motor. Texas direct auto where I purchased it, was not helping me out as well. The Ford truck has a 3. 5l v6 dir dohc 24v (ecoboost) motor. I know that NHTSA is/was investigating on these motors. I can not afford a $10,500 motor plus a paying for a $29,000 truck note.
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Engine started making a loud noise upon inspection of engine found that the back spark plug on passenger side had blown out from head and of course stripped the treads from the head the spark plugs are the ones that came from factory they have never been removed or replaced vehicle was purchased new after reviewing information on the internet this seems to be a major problem with Fords 4. 6 and 5. 4 engine as well as resulting in fires and considering Ford makes a repair kit. If this has effected this many vehicle shouldn't Ford foot the bill.
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While driving at 65 - 70 mph on I-95, the spark plug on the #2 cylinder blew out. #2 cylinder is 2nd plug from front of engine on the passenger side. Loud noise and lost power.
Tl- the contact owns a 2004 Ford F-150. The contact stated while driving approximately 65 mph, the engine stalled without warning. The contact noticed that the vehicle would intermittently have a sudden increase in engine rpms and a loud noise was present. The failure recurred multiple times. The vehicle was taken to various independent mechanics. The technician stated that the wiring harnesses and cam phasers needed to be replaced. In addition, the intake and throttle body needed to be cleaned. The vehicle was repaired. However, the failure recurred. The manufacturer was notified of the failure and the approximate failure mileage was 120,000. The VIN was unavailable. Pam.
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As I was driving home, my engine began making a loud noise & running badly. Upon inspection of the motor, I found the spark plug had blown out of the #3 cylinder, breaking the coil pack in the process. I do not believe this is a normal occurance. I have checked on-line to see if this has happened to other F-150 owners, and found out it is fairly common. What can be done to get Ford to help with this problem?.
The contact owns a 2007 Ford f150. The contact stated that while driving 35 mph, an abnormal noise was heard from the engine as the vehicle suddenly stalled. The contact was able to restart the vehicle and took it to an independent mechanic, who diagnosed a lack of pressure on the right side of the engine. In addition, water from the cooling system had leaked into the engine. The vehicle was not repaired. The manufacturer was notified of the failure. The failure mileage was 84,000.
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The contact owns a 2002 Ford F-150. The contact stated that while driving 35 mph, the vehicle made a loud noise. The vehicle was taken to the dealer where the technician diagnosed that there was a blown spark plug that needed to be replaced. The manufacturer was made aware of the failure. The vehicle was repaired. The VIN was not available. The failure and current mileage was 170,000.
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The contact owns a 2006 Ford F-150. The contact stated that the vehicle was started and the engine exhibited a loud noise. Additionally, the contact smelled a burning odor. The contact took the vehicle to a local mechanic, who stated that the spark plug had melted due to the heat from the head gasket. There were no repairs made to the vehicle. The failure mileage was 40,000.
Driving down the highway and heard loud noise and truck came to a stop, pulled off safely to side of the road found out it was misfire in cylinder 2. Only have had truck for 5 months now needs a brand new engine.
The contact owns a 2002 Ford F-150. The contact stated that while driving 40 mph, he heard a loud noise as the vehicle began to shake violently. The vehicle was shut off and restarted however, the engine roared abnormally loud and exhibited a reduction in engine power. The contact found a spark plug sitting on top of the engine, which appeared to have been ejected from the engine. The vehicle was not diagnosed. The manufacturer was notified and stated that no assistance would be offered. The failure and current mileage was 149,500.
Tl- the contact owns a 2002 Ford F-150. The contact stated while driving 60 mph he heard a loud noise under the hood. He then noticed gasoline spraying out of the vehicle. After further inspection he noticed a spark plug had blown out of the head of the motor. The vehicle was towed to an independent mechanic for diagnosis and was informed that the aluminum in the block was not strong enough to hold the spark plug and that it was a common problem. The hole was re-threaded and a sleeve was placed inside. After 50 miles the failure recurred. The vehicle was towed to a different mechanic and he was awaiting diagnosis. The manufacturer was notified but offered no assistance. The vehicle had not been repaired. The failure and current mileage was 137,000. Dt.
Vehicle began to smell like gas in the cab on numerous occasions. Took it to Ford dealership mechanic and was told that the source of the gas smell could not be found. A few days later upon starting the vehicle, a very loud explosive sound was heard under the hood. The vehicle was turned off and towed back to the Ford dealership where it was determined that the original #2 spark plug had blown out of the engine and damaged the head. Repair exceeding $700 with absolutely no responsibility taken by Ford. Repeat incident less than one year later with another cylinder.
My 2011 Ford F-150 ecoboost 3. 5 was idling at a red light then suddenly began a very rough idle. This went on for about twenty minutes ( on and off) then cleared up . We took the truck to the local dealership and had them look at it . They did a service order and came up with nothing wrong. We took the truck home and the problem remained. The truck was taken back 4 or 5 more times for the same problem and the dealership could never find a problem. While driving the vehicle on the highway and attempting to pass slower moving cars, the truck hesitated and sputtered when the gas pedal was depressed. A month ago the engine started making a noise after a cold start and then lately a louder noise from time to time in the passenger side front area of the valve cover. Then the truck just stopped on me while on the highway . I had it towed to the dealer and now we are talking about a new engine? what the ????? it has 50k and the oil was changed regularly, but the dealer is saying there is sludge in the oil which was changed less than 2000 miles ago. The timing chain is stretched, the intake cam vtc is broken and based on all of the other similar post I've been reading about this same issue they have revealed that the rod and cam bearings are also more than likely prematurely worn, requiring a new engine to repair the damage.
Tl-the contact owns a 2005 Ford F-150. While driving approximately 50 mph, a loud noise emitted outside of the vehicle. The contact maneuvered to the side of the road and then resumed driving. The vehicle was inspected upon arriving to the residence. The contact detected the number seven spark plug dislodged from the engine cylinder head. The authorized dealer was notified and they informed there was not a recall pertaining to the defect. The vehicle had not been repaired. The manufacturer was not made aware of the failure. The approximate failure mileage was 115,000. Js.
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The contact owns a 2009 Ford f150. The contact stated that after starting the engine, there was a loud, abnormal noise emitted from the vehicle. The vehicle was taken the dealer who was unable to diagnose the failure. The manufacturer was made aware of the failure but did not offer any assistance. The failure and the current mileage was 59,000.
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Originally factory installed sparkplug blows out of the engine head traveling at approximately 35 mph. This was disclosed after taking vehicle to a Ford dealership for diagnostics as there was a loud noise while engine running and loss of power. Repair cost was $617. Discussion with dealer discloses that this a well know problem by Ford management, a tbs has been issued. Further Ford has denied any responsibility and will not provide any monetary assistance. This is a Ford created design engineering defect that Ford just ignores and let's the customer pay for its mistake. Customer is subject to cost of repair that is far from normal wear and tear, a safety concern of fire in engine compartment from raw fuel blown out of the hole vacated by sparkplug, a reliability issue and a safety concern from sudden loss of power. This problem should be covered by a federal mandated recall since Ford is making this a consumer problem ignoring the fact that it is a engineering, design or manufacturing problem for which it refuses to accept responsibility. In addition the trade in value of this vehicle will be reduced by the Ford dealership that is aware of the problem evan for the customer that did not encounter a sparkplug blowout and at private sale if prospective buyer checks on vehicle via any internet automotive site. Again Ford lets consumer absorb cost of defect it created.
The contact owns a 2007 Ford-150. The contact stated that when he came to a complete stop, he heard a loud noise coming from the engine. The vehicle was taken to a dealer, who diagnosed that the timing chain needed to be replaced. The vehicle was repaired. The failure was recurring. The manufacturer was made aware of the problem. The approximate failure mileage was 152,000.
My vehicle is equipped with the 3. 5 liter ecoboost 6 cylinder engine. Upon attempting to pass a vehicle while traveling at freeway speeds, the vehicle began to hesitate and the engine felt rough. The vehicle refused to accelerate, causing me to swerve back into the right lane to avoid being rear-ended by a vehicle traveling in the left lane. After approximately 30 - 60 seconds, the vehicle would accept throttle and resume normal operation. This problem has repeated itself on multiple occasions and my vehicle is currently at the dealership for the 7th time to remedy this problem. In only one instance of the many that I've had, I did get a check engine light on. Fortunately, this was documented by the Ford dealership as one entire bank of cylinders misfiring. Additionally, I have been complaining of transmission shift issues, where at slow (less than 10 mph) speeds, the transmission often 'hunts' between two gears and once selected, a loud noise emanates from under the vehicle and causes the vehicle to noticeably jerk I only learned of NHTSA pe13018 on 1/28/15. The first incident yielded installation of the deflector in the vicinity of the charge air cooler. Another incident yielded a TSB to remove the deflector, and most recently another TSB to re-install said air deflector. In every instance of this problem, I've had to execute emergency maneuvers to avoid traffic accidents. The service manager at my local Ford dealership has commented that Ford engineering has no clue how to remedy this issue. My vehicle currently has approximately 75,000 miles on it and is covered under Ford's extended warranty.
The contact owns a 2005 Ford F-150. The contact stated that while the vehicle was parked, a loud pop noise was heard and the vehicle erupted into flames. The vehicle caused extensive damage to a commercial building in which it was parked near. The police were contacted and a police report was filed. The fire department did not determine the cause of the fire. The manufacturer was not contacted. The failure mileage was approximately 78,000. Updated 03/28/12 updated 03/30/12.
The contact owns a 1998 Ford F-150. The contact stated that the vehicle stalled without warning, accompanied by a loud noise from under the hood. The vehicle was taken to a mechanic for inspection where the contact was advised that the spark plugs did not have enough thread and separated. The vehicle was repaired. The manufacturer was made aware of the failure. The failure mileage was 100,000 and the current mileage was 152,000.
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The contact owns a 2006 Ford f150. The contact stated that the engine exhibited an abnormal noise while driving at any speed over 30 mph. The vehicle was taken to the local mechanic who performed a diagnostic that located the failure at the number seven and eight spark-plugs. The mechanic advised that the spark plugs had separated from the holder and caused a piece of the spark plug to penetrate the engine. The vehicle was not repaired. The VIN was not available. The failure and the current mileage was 116,000. Updated 10/27/lj updated 12/06/2011.
The contact owns a 2002 Ford f150. The contact stated while the vehicle was parked he heard a loud noise and noticed the vehicle was on fire. The fire department stated the fire initiated in the engine. There was no mention of a fire report being filed. The VIN information was not available. The failure and current miles was 200,000.
The contact owns a 2005 Ford F-150. The contact stated that while driving, he heard an abnormally loud noise from the vehicle. He inspected the vehicle and noticed that a spark plug from the cylinder block had ejected. The vehicle was taken to the dealer who verified the failure and stated that the block needed to be re-threaded. The manufacturer was made aware of the failure who did offer any assistance. The vehicle was not repaired. The failure and current mileage was 120,000.
The contact owns a 2000 Ford F-150. The contact stated that he heard a loud noise in his driveway, he went outside and the vehicle was engulfed in flames. The contact did not mention if there were any injuries. The police were called and a report was filed. The vehicle was not inspected by a dealer nor was it repaired. The manufacturer was contacted and advised him that the legal department would contact him. The failure mileage was approximately 175,000.
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I was driving on a highway at 55 mph in my 2004 Ford 150 when I heard a loud noise from the engine. Found a spark plug had been completely blown out of the engine. I have done some reading and found this to be a common problem with Ford's triton engines. Coil pack was sparking which could have led to a serious engine fire. Please have Ford fix the problem.
I have a 2001 Ford f150 crewcab truck. On my way home from work, my vehicle started making an awful noise and the truck instantly started working rough. I pulled over and turned off the truck. My husband came to check on me and when we popped the hood and when I turned on the truck he saw the spark plug coming out of the cylinder. I have yet to have the mechanic look at it. After reading up on this, I see this is a recurrent problem on Ford trucks. I do not understand why nothing has been done regarding this matter. I simply do not have the funds available to pay for this if it is a major repair job nor do I have the means to purchase another vehicle due to the current economic state and were barely getting by as it is. I want something to be done and this issue with Ford investigated further. It is a design flaw and this is getting ridiculous. Do someone have to die in order for something to be done. Thank god I did not pick my kids up yet . Thank god I was just starting off from a light and hadn't even got back up to 20 mph. Thank god it happens to me and not my husband that drove out to orlando today and was going to use my truck. He would have been severely hurt or worse if this occurred at 70+mph. I have read that this could cost in the thousands and when I get an estimate I will update this matter further. Something has to be done, there are no more excuses.
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The contact owns a 2004 Ford F-150. The contact stated that the vehicle would make an abnormal noise while in motion. The dealer diagnosed that the cam-phasers would need to be replaced. The manufacturer was notified, but denied any assistance with repairs to the defect. The vehicle was not repaired. The failure mileage was 110,000 and the current mileage was 117,000.
The contact owns a 2006 Ford f150. The contact stated there was an abnormal noise coming from the vehicle rear when performing a turn. The vehicle was taken to a local repair facility where repairs were made to the vehicle. The failure recurred within two weeks. In addition, the contact stated that the vehicle would not start. The vehicle was not further repaired. The failure mileage was 80,000. Updated 12/01/10. The consumer stated there was still a noise coming from the vehicle. Also, the vehicle would not start on several occasions. Updated 12/14/jb.
The contact owns a 2005 Ford f150. The contact stated that while driving 60 mph, a loud noise was emitted from the engine compartment. The contact mentioned that the failure recurred twice. The vehicle was taken to the dealer who diagnosed that the spark plugs were not torqued correctly, causing the spark plugs to be spewed from the engine block. The manufacturer was made aware of the failure who did not offer any assistance since the vehicle was not included in any recalls. The vehicle was repaired. The failure mileage was 87,000 and the current mileage was 120,000.
Event. . I was driving west bound on the 215 freeway in las vegas, nv. Exiting durango road. I sat at the intersection waiting for the signal light to turn green. When the light turned green, moving forward, I was making a left hand turn going (10mph) south bound on durango road, just at that time I herd a loud pop noise. As I was pulling over, my truck (f150) was running rough, I stopped, put it in park , shut the engine off, opened the hood and there sat a coil pack including the spark plug on top of the motor. After evaluating the incident more, I notice that the coil pack and spark plug came from the passenger side engine head #three (3) cylinder. My truck has the original motorcraft spark plugs in it since 2002. Not sure why the spark plug would just pop-out. Nice job Ford!! Ford manufactures the motor (triton 5. 4l) and the motorcraft spark plugs? seems very simple whose responsibility this is. Repair costthe repair shop is estimating $2,500. 00 head repair or new engine at approximately $6,500. 00 inc. Labor. Questiions. . How is the consumer going to know prior to the spark plug popping out, to secure it? why are the spark plugs popping out? not enough threads? how do the executives at Ford sleep at night knowing that this problem could take someones life at any time? personal comment. . When the spark plug or the coil pack was ejected from the engine head, this could have hit the fuel rail and started a tremendous fire, like a lot of people in the us we dont always carry a fire extinguisher because an !@#$% spark plug is going to pop out of the engine head and start the truck on fire. This is ridiculous!!!! Ford motor company needs to own up to there mistakes before somebody looses there life. I am not the suing type of person, but if one of my kids looses there life driving my truck because of a spark plug problem and Ford motor company did not tell me about it, I am afraid to tell you what I would do. This is not a threat just reality.
I own a 2002 Ford F-150 XLT 4x4 with a trition 5. 4l v-8. I went out to start it this morning and I heard a loud noise that sounded like a shot went off. Then my truck started shaking and making a chugging noise. I shut it off and opened the hood and found that one of my spark plugs just blew out of the engine. It broke the coil and stripped out the threads where the spark plug goes. I had to have it towed to a mechanic and it cost $503. 83 for the repair. The mechanic told me this was a common problem with the trition engines. I went online and did some research and found many complaints of the same subject. I think Ford needs to issue a recall to fix this problem.
My Ford-150 pick-up started making a small noise for a few days. I went out to start my truck and it no longer was a small noise but one big loud noise. I had my oil and plugs changed on October 15, 2008. Upon raising the hood I found that one of the spark plugs had blown out from where it was suppose to be. The plug looked like it was the old one and that made me think that they had not changed my plugs. The truck was towed to the dealer and he informed me that the plug was one of the new ones but that the head hid blown the plug out. (I hope I am saying this right). The service manager told me that there had been a lot of problems with this happening to the Ford trucks but that no recall had ever been issued. It seams that there is some weak spots due to the metal not being strong enough to hold the plugs in. I have been researching this problems and there are a lot of people complaining about this same situation.
On 10/5/08, driving near home, slow speed, heard a loud noise from under the hood, lost power. Determined that the 4th spark plug on drivers side had unthreaded from engine, damaging coil. On attempt to replace with new spark plug, learned that the cylinder head threads were damaged (stripped). 76,000 miles, spark plug had never been removed, was original from Ford factory.